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The launch profile as planned had the booster shutting down at 169 seconds.

In the event, it burned for 239s, or more than 40% longer. We know that the booster lost 5-7 engines during the flight, accounting for less than 22% of the engines. I would expect the burn time to increase by less than 30%, and more like 20%

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    $\begingroup$ I don't know if this was the reason, but don't forget that the booster had a substantial reserve of propellant to be used for landing, which it could instead use in an attempt to get the upper stage to orbit if problems occur (as the Falcon 9 has done). $\endgroup$ Commented Apr 22, 2023 at 18:16

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How did it burn so long? Because it was loaded with way more fuel than required for the planned burn.
Why did it burn so long? Because it was trying to make orbit with less thrust.

If some of the engines don't fire, then the lift takes longer, and every second it spends in the atmosphere represents more energy lost to drag and more fuel spent to counteract gravity instead of accelerate the rocket. So if you lose an engine, you need more fuel than planned in order to reach the desired speed and altitude. If you lost an engine but burned the same quantity of fuel, you'd end up low and slow.

The extreme case would be if you lost enough engines that you're precisely countering gravity with no extra thrust, in which case you could spend an infinite amount of fuel without ever reaching orbit because you'd just be maintaining your speed but not getting any faster. (Technically that wouldn't happen because the rocket is getting lighter as it burns fuel and gravity drops off as you move away even if you're only maintaining current speed, but it should help clarify why you burn more total fuel when your thrust output is lower.)

The Superheavy was loaded with a good bit more fuel than required for the planned burn. The flight plan included having the booster perform a boostback and simulated landing after stage separation, so it could cut into the fuel meant for its return trip in order to try to complete the primary mission. Even beyond that, they may well have launched with more fuel than needed for the planned mission -- there are reasons to launch with a nearly-full load of fuel instead of half-a-tank, such as the structural stiffening that comes from having the tanks closer to full. In any case, they had plenty of extra fuel aboard. When the engine cluster started badly underperforming, the rocket automatically adjusted its angle and extended the burn time in an effort to reach the intended altitude. As the flight goes on, you can see in the telemetry that the angle of attack starts to go higher and higher as the rocket aims its nose upward instead of directly into the airstream.

Eventually either it overcontrolled, getting the angle of attack far enough off center that it could no longer maintain the position against the aerodynamic forces, or it had been leaking hydraulic fluid (possibly due to damage from debris thrown up when it wrecked the launch pad) and the gimbals got unresponsive, or both, or some third thing, but in any case it wasn't able to maintain orientation (the Starship/Superheavy stack is inherently unstable due to Starship's winglets) and it started to tumble.

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    $\begingroup$ I think an important note is that it's not necessarily that it had extra fuel/oxidizer for engine-out capability, but it was also intended to do 3 burns in total. Burn 1, 169s, burn 2, 55s, burn 3, 23 seconds. See schedule here. Those burns might have also been expected to use fewer engines and so also use less fuel, but in general, I think they may have eaten into their boostback & landing propellant budget due to the loss of engines (for the exact reasons you mention). $\endgroup$ Commented Apr 22, 2023 at 19:37
  • $\begingroup$ That's true, I didn't think about the boostback and landing, they certainly could have been cutting into their landing fuel supply to try to hit the orbit. But I think I remember some discussion before the launch that they were probably loading way more fuel than needed for an empty Starship because it would weaken the structure and they would want it as sturdy as possible for the first time through max-q. Of course it's all speculative unless SpaceX decides to talk about it, they don't exactly divulge all the details of their engineering. $\endgroup$ Commented Apr 22, 2023 at 19:50
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    $\begingroup$ I saw the tumbling on the video and wondered why it wasn't destructed nearly immediately - it seemed to go on for quite awhile. $\endgroup$
    – davidbak
    Commented Apr 23, 2023 at 17:52
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    $\begingroup$ @davidbak as long as it's in one piece, the lower the altitude it destructs at the lower the area affected. It was likely destroyed when it started to fail structurally or when the estimated impact point got too close to the borders of a defined ground area. $\endgroup$ Commented Apr 23, 2023 at 20:29
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    $\begingroup$ @ChristopherJamesHuff - indeed. A lot of people seem to expect FTS to be triggered at the first sign of a problem, but the purpose of FTS isn't to blow the rocket up... it's to prevent it from endangering things outside of the exclusion zone. Having it doing somersaults in the air is obviously a problem for SpaceX... but it's not actually a safety issue as long as it doesn't go out of bounds. $\endgroup$ Commented Apr 24, 2023 at 0:08
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We don't know for sure. But it seems likely that the software would be programmed in such a way that the prime focus would be to get Starship into orbit at all costs.

So if any engines were lost it would burn the remaining engines for longer to make up for it. If for whatever reason, the correct altitude and velocity were still not achieved, I imagine Superheavy would burn its reserve propellant intended for retro propulsive landing and then any safety margin and then just keep the engines firing until they literally ran out of LOX or methane.

If at that point the correct altitude and velocity were not achieved what then? Who knows? The final default position might have been to simply leave Starship attached on the basis that it would be better to have one giant cartwheeling out of control rogue rocket than two.

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    $\begingroup$ I think the most important is the verdict on the Raptor engine and the 33 engine configuration in Super Heavy. Is this a working design, potentially powerful enough for a Starship ? $\endgroup$ Commented Apr 24, 2023 at 14:18
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    $\begingroup$ Performance exhibited by Super Heavy during the test flight was rather weak even though Starship was without cargo and fuel for landing. We can make an assumption about sustained damage and 5 engines out, but still. $\endgroup$ Commented Apr 24, 2023 at 14:24
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    $\begingroup$ On the third minute of flight when 1/2 of the propellent were gone, Super Heavy should have shown more agility, even without 1/6 of the engines. $\endgroup$ Commented Apr 24, 2023 at 14:39
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    $\begingroup$ Do they have to rethink the design of Super Heavy? $\endgroup$ Commented Apr 24, 2023 at 16:55
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    $\begingroup$ @Star-SpaceX They are always rethinking the design of Superheavy, it's just that the changes tend to get smaller as time goes on as the refine it. They won't have to start the design again. $\endgroup$
    – Slarty
    Commented Apr 25, 2023 at 8:55
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The booster had enough fuel for the 169 second burn you mentioned plus boostback and landing burns, and likely likely some contingency fuel in the case of for loosing engines.

Each engine produces about 3% of thrust but what matters for acceleration is the amount by which thrust exceeds gravity. This means that while each engine contributes only 3% of thrust Starship's acceleration decreases about 10% for each engine it looses (the exact amount depends on how much fuel is left). Starship was out three engines immediately and rapidly lost more, with others showing signs of malfunction. Therefore, it was down a lot on thrust and would have needed a far longer burn to reach orbit.

The priority will have been to get starship to orbit, rather than to land the booster. Therefore the code will have told the engines to keep burning in the hope of getting enough speed to release starship.

In the final event the booster didn't achieve the necessary velocity and starship wasn't released. However, to the best of my knowledge it's unknown if this was intentional or not, releasing starship and firing it's engines would have provided a lot of useful data even if there was no chance of it reaching orbit but it also could have been judged too dangerous to release it. Therefore, both a malfunction and a decision not to release are entirely plausible.

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